GOODYEAR HEAT EXCHANGER RUPTURE CASE STUDY

GOODYEAR HEAT EXCHANGER RUPTURE CASE STUDY

All reports may contain safety recommendations when appropriate. However, whether this occurred during the June 10 dayshift is unclear, and Goodyear was unable to produce a signed copy of the work order. It is also important to have redundancies in a pressure relief system so that any individual equipment ruptures do not compromise the safety of a given process. Marketing mix decisions such as communication, promotion, distribution, pricing, etc. CSB Safety Bulletins are short, general-interest publications that provide new or noteworthy information on preventing chemical accidents. This product coming to light would put the company back on the road to success and gain back the trust of exchanger consumers.

Operating procedures discussed plantwide, alarm operations and emergency muster points for partial and plant-wide evacuations; however, some employees had not been fully trained on these procedures. The operator, who carried out rupture exchanger tube cleaning with steam, did not fully understand the properties of chemical, in this case ammonia. January Pressure Vessel Standards 3. When rupture below the diaphragm of this actuator becomes greater than the pressure above it, the diaphragm will move upward and the valve will open. The catastrophic rupture threw debris that struck and killed a Goodyear employee walking through the area. In the production area, a series of reactor vessels process chemicals, including styrene and butadiene.

Actuators can be pneumatic, meaning they use pressurized air to regulate valve opening and closing, or electric, which goodyear exchanfer power for regulation. The pneumatic diaphragm actuator, shown on the left below, is attached to the top of a valve. Piping carries product from the reactors to the product finishing area.

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Ammonia vapor irritates the eyes and respiratory system and makes breathing difficult. Copyright Chemical Casse, Access Intelligence, LLC Relief Devices in case relief systems open at a preset pressure so that excess pressure and the contents causing that excess pressure can be relieved from a heat.

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goodyear heat exchanger rupture case study

These devices open and close based on an study signal sent from a controller. Goodyear uses pressurized anhydrous ammonia in the heat exchanger to cool the chemicals used to make synthetic rubber. Hours later, workers discovered the victim buried in the rubble near the ruptured vessel.

However, in order for the company to make this new product successful they must rxchanger a powerful marketing strategy.

Plant personnel were not provided with the proper training to effectively manage this emergency. Immediately after the rupture and resulting ammonia release, Goodyear evacuated the plant.

Goodyear heat exchanger rupture case study

The next day, at about 7: To the right of the pneumatic diaphragm actuator is an electro-mechanical actuator, which controls valve opening by receiving an electrical signal which activates a motorized gear that changes valve opening position.

Ammonia vapor returns to the ammonia cooling system where it is pressurized and cooled, liquefying the ammonia. The operator then connected a steam line to the process line to clean the piping. Because the over-pressure protection remained isolated, the internal pressure increased hsat the heat exchanger suddenly and catastrophically ruptured.

Chemical Safety and Hazard Investigation Board CSB is an independent Federal agency whose mission is to ensure the safety of workers, the public, and the environment by investigating and preventing chemical incidents.

Goodyear heat exchanger rupture case study / paper writing help online

However, when the valve was in the closed position, the heat exchanger was still protected from an over-pressure condition by the automatic pressure control valve.

More information about the CSB is available at www. Maintenance workers replaced the ruptkre disk on that day; however, the closed isolation valve was not reopened. Control Valves Control ruptures are the final control element in heats pressure control systems. Chemical Safety Board CSB case study released today on the heat exchanger rupture and ammonia release at the Goodyear Tire and Rubber Company in Houston, Texas, identifies gaps in facility emergency response training and calls for increased adherence to existing industry codes.

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One very important rupture of pressure exchanger devices is how they are exchnager.

Medical responders transported the six injured workers. Goodyear heat exchanger rupture case studyreview Rating: One cubic foot of liquid ammonia srudy cubic feet of vapor. Managers ordered the plant evacuated. The vapor can also remain close to the ground when it absorbs water vapor from air in high humidity conditions.

As the ammonia absorbs heat from the process chemical flowing through tubes in the center of the heat exchanger, the ammonia boils in the heat exchanger shell Figure 2.

goodyear heat exchanger rupture case study

CSB Case Studies are short reports on specific accidents and include a discussion of relevant prevention practices. During the incident however, a malfunction in the badge tracking system delayed supervisors from immediately retrieving the list of personnel in their area. On the day prior to the accident, maintenance work required closing several valves on the heat exchanger. However, CSB investigators found that on the day of the accident the employee tracking system was not operating properly, making it difficult to quickly account for all employees.

Goodyear uses three ammonia heat exchangers in its production process lines. Only the immediate area involved in the rupture remained evacuated.